and CP/M was chosen for two reasons. Firstly the University of York
Electronics Department were prepared to offer a support service for
such à machine, and secondly it was known that an 'off the shelf'
interface was available which would work with this specification of
machine. There are a bewildering variety of microcomputers available,
even within this specification, all with their own claims to have some
unique feature. The North Star seemed to offer good value for money,
plus a local agent for servicing.
Interface
The interface used between the encoders and the microcomputer was an
"off the shelf' item manufactured by Soton Micro Systems. Most of the
electronic components for this interface are on one card which slots into
the North Star S100 bus. A separate power supply unit is needed to
provide current for the encoders. The coordinate display and menu are
shown only on the VDU. There are no separate counter displays on nixie
tubes or LED etc, The software supplied as part of the interface
'package'! provides a range of options for recording in point, time or
distance mode, and facilities to insert headers before strings or
coordinates, etc. A certain amount of alteration to the software had to
be carried out by the manufacturers to make it operable with the North
Star/Hazeltine combination. Coordinates can be stored onto either of the
disks, or output to another device if wanted.
OUTPUT
The function of the output system is to electrically drive the Thompson-
Watts Coordinatograph table through stepper motors. This output is
perhaps the more interesting part of the whole system, as it shows how
for a very modest cost, an existing coordinatograph table can be driven
electrically. Fig 5 shows a general view of the coordinatograph table,
with the stepper motor unit attached.
Fitting the Stepper Motors
The 'X' and 'Y' shafts of the coordinatograph conveniently projected about
15 mm from the body of the table (Fig 4). A drive system was designed
using a flexible toothed nylon belt, working with a two to one reduction
(Fig 6). This allowed the motors to be set back so (Fig 7) that they did
not project unnecessarily, and also allowed much lower tolerance in the
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